I finally think I fixed the issue which was rooted not in the quadcopter, but in the controller. I was adjusting settings mid flight and one of the switches had been changed from hold to gear. I have no clue what gear does, but hold seemed to make the quadcopter hold in place when I hit the right switch. I didn't have a ton of time to test it, as it was freezing cold outside, but I think everything is finally working. If I have the recourses, I might start and try and get into 3D modeling with my drone next!
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AuthorMy name's Chris, I'm a high school student who likes food, sleep, video games, and quad copters. Archives
January 2017
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